First id like to say im stripping the car from the interior removing anything that would be useless in car. This car will only be for drag use and week-end drive bye. Engine is out (no oil pressure) the compression was 120 cold all across 6 piston some det on 1 the head gasket was cracked and prestone went in oil pan. I smell a rebuild. This is a project so it may take a while but i want to go back to the drag strip by next summer. Im thinking of 2.8L stroker HKS T51RSPL TURBO setup. Parts i have OS GIKEN triple plate clutch AEM EMS Uego with 3 gauges Trust fmic Grex oil cooler relocator oil temp,oil pressure Omori gauges splitfire coils iririum plugs Z32 MAF cusco front rear strut bar rollcage. There is a aftermarket fuel pump i don,t no what it is but it push my 1000cc Rc inj. two lines that go to the pipe at both ends one was tap in close to the firewall. Turbo set up was twin HKS2530 with Apexi power fc tune to 422WHP and best quarter mile was 12.34 at 117mph. Now with the Aem i figured i would have been in the 11 for sure with slicks. But now ill never know cause im rebuilding block so i need advice on what im going to keep on the car and make it light on her feet.
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LeKing Drag GTR Project
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This is my motor when i just bought the car in september of 2007. Yes hard HKS piping came with the M's cone filter makes a nice polish look. Notice that they had put 2 filters on the blowby valve covers.hummm interesting!!!
Then 6 days later I went for a few 1/4 mile pull. It did not go as plan. My rear turbo needed to be rebuild. It was spooling really weird almost puffing this was really disapointing but i just knew there was something special with this one.
HKS 2530 yes sir all cleaned and rebuild.
Painted my manifold with high heat temp paint had to cure on top a wood stove they came out pretty good.
Now to put it all back in.
After it was complet i had to check for leaks . Prestone was gushing out from under neat of the car what a mess. Freaking oil leak also made it a pain those press copper washer were used or something it did not seal properly even to this day i still have some leaks because of those copper ring. Installing turbos and manifolds is so a pain in the ass u absolutely have no room and after u have to torque these bolts holly crap . Now i wish i should of pull the motor out u have to drain block anyways. O well there's always next year.
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When i got the car it came with a stupid shift knob everytime i shifted the knob was coming off. I really like the Nismo carbon fiber look so i went with that. I decided to buy a C's short throw kit from Nengun it really shorten the throw and help me shift left handed . I needed a oil filter so i baught a trust oil filter and a nismo radiator cap. That was my first order from japan.
Time for her first oil change AMSOIL
So in the winter i ordered with RHD japan Apexi Power FC,SplitFire coils and a HKS manifold gasket set since i needed to put my turbo's back in. I installed my Innovate wide band gauge were my Omori water temp was since its not working and i can now monitor it on the power fc. Now she's coming along just like i want to just before i go on the Dyno. You'll notice i removed the leather trim from the hand brake and shifter they were cracking so out to the garbage they went.
Here is pics of my engine before and after.
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YES TW those breather have now been change especially the one on the turbo side would let blowby over my turbo. Image me and my wife driving along we accelerated pretty good meening it boosted so i see smoke coming from the dash it s like WTF....oil dripping on the rear turbo to the downpipe was burning and was able to creep where the tranny is to the ashtray console. Quite funny now but at the time it's like is there a short or what.HAHA
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So now i was ready to go to the dragstrip until this happen.
PACMAN
OSGIKEN twin plate
Since i had no clue of how much hp this car was making. I decided on buying a triple plate.
looks nice on my car
Since now the car had cost me a few $$$$ to repair i decided to go on the Dyno get her tune right and then next year ill be ready to go on the drag and see how she does on the 1/4 mile.
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Finally took a day off work to get her to JD Racing on the dyno.

We were all strap in to find out the HP# of my "GODZILLA".

Woops!!! Burn one of the rear straps sorry dude!!!!

Then we finally got what i was waiting for dyno result. This is on stock injectors Z32 maf SplitFire coils HKS 2530.
YouTube - GTR Dyno 422whp

The next morning we arrived and Danny had already installed my Rc eng.1000cc injectors and he was ready to tune.


I finish the day with a big smile on my face since he gave me a drive in his 600whp integra and a few words of advice from Danny. He said the best thing u can do is fix your boost creep by doing this you'll be able to get your full boost by 5000rpm this will change your dyno graph like it should be. I was getting boost creep and only getting like 19 psi at redline. This was cause by my adjustable arms on my actuators were set to long i figured that last year.
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422whp on stock injectors is a bit risky imho... they are only 444cc. that powerband looks odd too for 2530s... since they are supposed to perform similarly to 2860's, i feel like you'd expect less of a linear powerband like yours ended up.. check out mine or luckygtr's. i hope the guy that posted above me isnt right
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No more nonsense about the shop, if you have a problem with someone take it up via PM. All the posts not referring to this project have been deleted.Sign up for GTRC Premium Membership and get 2 of the new GT-R Canada stickers!
http://forums.gtrcanada.com/general-skyline-discussion/45662-gtrc-premium-membership.html#post437410
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No worry, the 422whp is maybe "bloated" where other dynos may show less that 400whp. My car was found as 264whp or something but didn't turn past 210whp on a dynapac soon after. Either way, nice numbers but I'd find out what duty your injectors are at WOT and go from there.Originally posted by TW View Post422whp on stock injectors is a bit risky imho... they are only 444cc. that powerband looks odd too for 2530s... since they are supposed to perform similarly to 2860's, i feel like you'd expect less of a linear powerband like yours ended up.. check out mine or luckygtr's. i hope the guy that posted above me isnt right
Black 1991 GTR. Serious garage stand mantle/parts car.
Black 1990 Pulsar GTiR. Sold
Silver 1989 GTR. Sold
Black 2010 Subaru WRX. Weekend warrior. Sold.
Black 2013 F-150 FX4 ecoboost. Daily driver.
White 2012 Ford Explorer Limited. Family wagon.
Sorry for my offensive comments, I r socially retard.
lolstart by having A ROLLING GTR then we talk u ******* mofo funzy little *****
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the dyno sheet that show there that was the first pull at night just too check out the hp no tuning done back in 2008
i doo beleive we change the injector after and tune back after in the morning and gain a tiny bit peek hp but alot in the mid range 30 hp more and 30 tq after the tune at the same boost level
also that graph show hp still climbing that because it had boost creep
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