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I'd say the gasket was going. And you said 2 studs were stuck in the head? Most likely they were either failing and backed off slightly, leading to a small leak.. Mine definitely didn't look THAT black when i pulled it off, but it's hard to tell because the coating on them is a black like colour.. That looks like carbon though, so failed seal or backing off studs could have been very likely..
Cylinder 1 and 5 seem most prominent.. Whats worse is that if there's trace on the rest of the manifold from there, then its a more substantial leak, but that would be very noticeable; noisy and a definite response issue.
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based on the fluids mechanics class mec335 (still remember that one?) port matching will reduce the KL factor alot (sharp intake, sudden diameter reduction), which will in turn greatly reduce the Head loss (HL)
I have USED manifold studs from my other block, best to get new though unfortunately.. Let me know though!
Check out the GTST Projects page and keep up to date with my build!
www.nelsonmx.wordpress.com
Like us on Facebook! www.facebook.com/NelsonMX
Any part inquiries can be forwarded to marc@nelsonmx.com
Ahh man today I decided to used two shorter, easy to change studs to put my whole setup back in then: SNAP another stud I was trying to remove broke in my hands.
this time, we broke the easy out in the hole... it took us most of the evening to remove it.
and we somewhat damaged the thread ....
we were able to retap itbut I'm not 100% confident on the depth of the thread.
both studs that snaped were the ones where there were signs of an exhaust leak on the exhaust gasket...
this one was like soldered into the head ... gaaaahhh
Man and I thought I was gonna have my turbo running tonight
Marc-André
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2.2L RB20 GTS-T ECU modification enabled - PM me for details
thats terrible man. i just did the same thing but i had 4 broken studs. i tried to use an easy out and they broke. so i have 4 broken studs 2 with easyouts in them. time to pull the head and send it to the machine shop...fml
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