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The R34 GT-T
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Nistune went well, stock turbo is tuned a bit high so I will back that off to about 12 psi.
Had some sudden loss of power the other day under load around 4000rpm, came to find my stock bov is leaking really bad. Which also means luckily I found this before my stock turbo started compensating too much and over boosting itself to hit the target boost fewhhhh!
Going to order a turbosmart plumb back bov to replace the old stocker, and then I may look into the actuator as well just in case.
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Originally posted by amnash View PostHow did you figure out it was the bov?
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